The first test run of the Steel and Glass cell suggested that it took approximately 6% more power to maintain the same volume of water at the same temperature in the control cell when compared to the active cell.
New Experiment Improvements
So, spurred on by the seemingly positive preliminary run of the Steel and Glass cells and taking a plethora of advice from the crowd, Nicolas sought to make some improvements to the experiment. The biggest revelation came from Celani, who informed us that the teens class wires (14 & 16L) that we used in the first run were actually the worst capability wires, this was explained in the previous blog post. So for this run, a new 14L wire was joined by a 360L wire.
You can see in the following images there were several improvements made to the experiment, many suggested by our followers. Chief of which was that the water containers were partially insulated with styrofoam boards.
Figure 1. Overview of the apparatus
Also, water stirrers were added and mounted in the same position and angle, pushing hot surface water down and creating a vortex.
Figure 2. View of stirrer blades set at angle in water and the driving motor mounted outside.
Water thermocouples were mounted on floaters to measure the water temperature at the same height from the water top level. This was ultimately found to be unnecessary, since the water temperature was very homogenous due to the action of the stirrers. In fact, the variation between bottom and top was only ±0.1°C.
In the image below, the laptop on the left is running HugNetLab for data capture. The PSU with the blue display underneath is powering the water stirrers (2x DC motors in series), whilst the Dell laptop on the right is managing the duty cycle for them.
The 2 TTi dual channels PSUs are powering the 4 wires.
- The top PSU is for Cell#2 (active)
- The bottom PSU is for Cell#1 (passive)
Figure 3. Arrangement of power, control and data acquisition hardware.
A complete gallery of the setup can be found here.
The Second Run
The second experiment was set up and run between 9 and 25 May 2013, the logbook of which is here
https://docs.google.com/spreadsheet/pub?key=0Au5C1oywPfSKdGhxM1F6ZGNwSmxOZUh3bEZyMmRMMHc&output=html
Unfortunately, whilst the data was recorded on a laptop, it was not able to be uploaded to the MFMP’s data repository due to what turned out to be a failed hard drive and a problematic software upgrade process. Until the data is available on-line however (which should be very soon), it is contained below in some spreadsheets for you to work through.
Here is the data for the wire loading in Cell#2 and the runs for both cells (11 days).
https://docs.google.com/file/d/0Bz7lTfqkED9WSkpVYjdrc3ZWNzQ/edit?usp=sharing
Experiment Configuration
For each cell
- 1 TC inside the glass tube for T_mica
- 3 TC in the middle chamber for T_glassout1, T_glassout2, T_glassout3
Cell#1:
- 2 Nichrome wires
- Hydrogen pressure: 2.054 bars @38.5°C inside the glass tube
- Helium pressure: 127 mbars @ 35.0°C inside middle chamber
- Input power: varies from 60W to 70W (30W to 35W in each wire)
Cell#2:
- Blue channel: 360L constant wire
- Red channel: 14L constant wire
- Hydrogen pressure: 2.054 bars @38.5°C inside the glass tube
- Helium pressure: 127 mbars @ 35.0°C inside middle chamber
- Input power: 60W (30W in each wire)
Preliminary Results for tentative discussion
Finding 1: Approximately 19% loading (0.81 R/R0)
Graph 1. Hydrogen loading related resistance changes over time.
Finding 2: There seems to be good evidence that more power is required to get the passive (control) cell to achieve the same water temperature as the active cell.
The graph below shows total input power for each of the cells (LHS) and the temperature of their corresponding water bath (RHS) over time. Cell 1 is the passive, cell 2 is the active. Annotations have been added to note events recorded in the log book. Note that the rate at which ambient affected the cells is relative to the water temp in the cells to begin with. Unfortunately, no ambient temp was recorded, but we feel there is some important information in the data anyhow.
Graph 2. Over view of power and temperatures in cells with logbook event annotations.
For detail purposes, the graphs below show how resistance changes in the Celani wires required power to be adjusted to maintain an approximate 60W total in the active cell.
Graph 3. Resistance change in active cell over time.
Graph 4. Fine power adjustments in active cell over time.
Preliminary Conclusion
We have an experiment design that is extremely easy to understand and that if the results hold up to scrutiny and are repeatable, we might have a suitable lab rat.
Further Work
In the next run, we will be using 2 X 400L class wires. We also intend to run for a longer period of time in order to get a more settled result. Ambient forcing and water level top up are problems seen in run 2, these are to be dealt with in the next test. The former by sitting the cells in chest freezers with the power off and the latter by sealing the tops of the containers.
We may later want to consider a mass flow variant of the outer shell which would allow accurate measurement as well as faster response times. Also, a larger inner cavity/more passthroughs would allow experiments on potential trigger and stimulation approaches.
UPDATE#1 - Last block of data available
As the data upload is taking so long, Nicolas has pulled the last block of data for this run from the laptop. To avoid you having to wait to see it, you can grab it from the link below, we'll try to find time to produce an annotated graph similar to graph 2 above.
Last block of data for run two
Please dig into the data and yes, we know that ambient would have been hugely useful here.
UPDATE#2 - Should we use a different heater?
So a few weeks back, whilst this run was underway, Celani phones us and says that he is stopping using NiChrome wires as "passive" wires in his experiments because of their potential to exhibit excess heat.
Questo indirizzo email è protetto dagli spambots. È necessario abilitare JavaScript per vederlo.&q=from:%22Jones+Beene%22" rel="nofollow">Whilst this should not be a problem for the Dual V2 protocol differential cells as there is no H2 in the passive cell under calibration or "active" run, it could be a factor in this experiment as the wires are in an H2 atmosphere.
One commenter called 'Jones Beene' on the Vortex forum alluded to this and suggested that we use some Kanthal resistance wire which is Iron-Chromium-Aluminium. This does not contain Nickel for certain, but it does contain Chromium, which according to Dr. Stoyan Sargs Basic Structures of Matter, Super Gravitational Theory's analysis, could be a very good candidate for the New Fire.
So, what to do. How about something radical. If the aim is to reach a steady state temperature in both water volumes, if we have them well sealed, stirred and well thermally insulated, how about just having a resistive heating element to heat the control water? Before you scream "different thermodynamics and time constants" well, that might just play to our advantage.
Think about it, it was difficult in the first two runs to match the active cell bath temperature because of the time constant being so long when making power adjustments to the passive cell. By the time the effect of the power adjustment had taken place the effect of ambient and potentially excess heat had made a moving target. Having a simple heating element would make the adjustments more immediate until the steady state of the overall systems were reached.
Ok, basically, maintain same power into active cell should achieve a target water bath temperature/rate of rise until steady state. Responsive adjustment to the heater element in the "passive cell" could allow rapid and responsive matching of its water bath. No LENR present in the heater element.
It has an added bonus of simplifying and reducing the cost of the experiment. Comments as ever below.
UPDATE#3 - New graph from second data tranche
Ok, so one of our followers produced a graph from the second tranche of data pulled from the laptop the other day, this is when things got closer to steady state and shows the importance of running an experiment like this for some time, here is what it looks like.
Active cell - input power RED (LHS), water bath temperature YELLOW (RHS)
Passive cell - input power BLUE (LHS), water bath temperature GREEN (RHS)
Graph 5. Fine adjustments of control cell input power to attempt to make its water bath reach active cells water bath temperature.
As ever, comments please!
UPDATE#4 - Exaggerated cool down graph
So it appears all of the data from the laptop is now uploaded to the online repository for people to explore in detail. It is interesting to note that data is recorded on the data logging laptops even if it cannot be pushed to the data repository, this proved very important given the failure of the harddrive in the array.
Below you can see the available data before the experiment was stopped of the cool down from steady state seen in Graph 5. The zoom in is further exaggerated because of the baseline being at 30, if it was 0, it would be very hard to distinguish any separation. There is however an extremely minor separation of much less than 1% over the 8 hour period. This indicates however that any thermal loss difference between the cells in the 3+ days of steady state in graph 5 when the control required 8.3 - 10% more power is not material to the indicative preliminary findings of this experiment.
Note: Ambient is actually the water bath temperatures on the data repository
Graph 6. Exaggerated cool down
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고모 보지가 오늘은 매말라 있었다.고모!
나... 하고 싶어.......? 나 졸리니
국산 야동 까 니가 알아서 해
음식을 섭취. 일주일에 세 번 우리 체중 코칭을 우리는 그것에 의하여서만 사용되는 우리의 체격 무게 저항입니다.
해야 당신이 결정하여 사용하는 각 유형의 기저귀를
가능하게 할 수 있는 젊은이는 십대에 넣어 pin-에 기저귀 바지 및 플라스틱을 위한 4nights 며 일회용 기저귀한 세 가지 일(또는 그 반대로)궁극적으로 어머니와 아버지를 해결 자체에 대한 여부는지를 모두 사용할 수 있도록 종류의 기저귀한 침대 자녀.
거기에는 또한 다양한 유형의 핀에 기저귀-prefold,
평면,와줍니다. 에 대해 더 깊이의 대화에 대해 완전히 다른 스타일의 천 기저귀조
제 7 장의 새로운 기저귀 프라이머입니다. 이
장은"로 알려진 기저귀 종류"그리고 협상에 관해서는 몇 가지 유형의 천
기저귀와 완전히 다른 종류의 직물 피복
기저귀로부터 제조될 수 있다. 에서 모두
금융 시스템 차원에 위치한 5 매트리스룸 휴 객실을 찾을 수
있습니다 바로 여기에 있습니다.
bit of it. I've got you saved as a favorite to check out new
stuff you post…
Part of the beauty of the thin wire is the small surface area for cooling. With 0.2mm wire at 1meter we have 6cm^2 surface area. This would be the same as a 1cmx1cmx1cm cube of powder (not very much powder).
One easy way to decrease the input power needed would be to replace the water with motor oil and heat it to 200 degrees C.
You are right on there. The idea is that we create derivative of this cell that is modular & flexible, allows powders and wire in the same unit as well as ways to stimulate or trigger it. So we would have high voltage and light guide passthroughs to allow arc/glow and laser discharge. Make the chamber length correct to allow for standing microwaves and have a mounting point for components inside the steel cell that could emit soft x-rays, microwaves etc.
Nano powder is difficult to control according to Defkalion as too much potential for thermal runaway - they got round this by using nano foam and triggering with glow discharge which not only heats but allows ionisation etc. Wire is too spread out for effective cross talk between hot-spots so in the "How many Celani wires can we fit in a tube" I propose in the comments that packing all but the monitor wires tightly together to maximize chances of thermal cross talk.
Also phonon resonance might play a role... once the right conditions are identified for sufficient thermal runaway, in a reactant geometry, duty cycle of stimulation or trigger will maximise COP.
Meanwhile what triggering experiments can be performed on the wire apparatus? plasma?
The one nagging question I still struggle with is why an apparently exothermic LENR reaction requires electrically generated heat to sustain itself. Is this because we have a coated wire substrate? ie. heat dissipation rate is too high for surface LENR reaction to be selfsustaining. or is the voltage gradient along the wire surface important?
Can't wait to see the data from your next runs.
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